9/25/13
Left longitudinal ready to be recovered.
Flipped chassis back over and spent this session finishing up some small welding details and prepping the rest of the compartment for sealer. Last welding detail was this small cross-piece. While not original it adds a lot more strength by tying the two flanges together to the heater tube. It also makes a nice mount flange for the rear seam of the new closing panel.
With that bit of welding done new closing panel trial fitments began.
A few refits, fine trimming and re-clamping were of course required.
It went surprisingly smooth however. I think mainly due to the fact that both end caps are off and out of the way.
It was so satisfying to begin to see this tube becoming sound once again.
Part of the adjustment phase was making sure all three of these mount flanges were aligned close enough to allow for a good fit of the eventual face panel.
Once that was established I spent the rest of the session prepping the cavity for a sealer coat. The surface rust I had to leave behind was treated with rust converter/stabilizer then a nice coat of epoxy 2k primer was applied.
While epoxy is good, primer always tends to be porous. For added protection I shot on a coat of paint. (spare stuff I needed to use up anyway)
Both paint and primer were thinned a bit more toward the end and spray concentrated up into the tight cervices.
Come along way from what it was...
I can now finally begin installing the new outer closing panel tomorrow.
Thanks for reading this! Justin
Left longitudinal ready to be recovered.
Flipped chassis back over and spent this session finishing up some small welding details and prepping the rest of the compartment for sealer. Last welding detail was this small cross-piece. While not original it adds a lot more strength by tying the two flanges together to the heater tube. It also makes a nice mount flange for the rear seam of the new closing panel.
With that bit of welding done new closing panel trial fitments began.
A few refits, fine trimming and re-clamping were of course required.
It went surprisingly smooth however. I think mainly due to the fact that both end caps are off and out of the way.
It was so satisfying to begin to see this tube becoming sound once again.
Part of the adjustment phase was making sure all three of these mount flanges were aligned close enough to allow for a good fit of the eventual face panel.
Once that was established I spent the rest of the session prepping the cavity for a sealer coat. The surface rust I had to leave behind was treated with rust converter/stabilizer then a nice coat of epoxy 2k primer was applied.
While epoxy is good, primer always tends to be porous. For added protection I shot on a coat of paint. (spare stuff I needed to use up anyway)
Both paint and primer were thinned a bit more toward the end and spray concentrated up into the tight cervices.
Come along way from what it was...
I can now finally begin installing the new outer closing panel tomorrow.
Thanks for reading this! Justin
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