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1959 356A S/R coupe project chassis # 108625

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  • Adjuster modification complete.
    Click image for larger version  Name:	IMG_9608.jpg Views:	0 Size:	199.8 KB ID:	113519 Basic hole elongation complete. Now onto fine file shaping.
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ID:	113520 Took a few tries but eventually got the shoulder of this grub bolt to slide snug and smoothly into its new space.
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ID:	113521 Block and bolt in full maxed out position.
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ID:	113522 Adjuster modification complete.
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ID:	113523 With this increased slotted hole size the block no longer covers and protects this opening completely from the eliments.
    Last edited by JTR70; 12-29-2022, 08:52 PM.
    Justin Rio

    Comment


    • Block modification:
      Click image for larger version

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ID:	113525 To shield this enlarged hole a pair of "Visors" like the example above will be added to both ends of the block.
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ID:	113526 This way no matter where the block is set the slotted hole remains covered top and bottom. Finishing out this last detail a bit later.

      Thanks for looking!

      Justin
      Justin Rio

      Comment


      • Cellette Bench Set up:


        I still have several loose ends to tie up in the engine compartment but in continuation with the chassis repairs I'm moving to the front of the car to confirm how much the front beam has been shifted from its previous front end collision. By the detectable deformation to the chassis behind the beam it isn't very much but while we're here we'll get it trued and blessed on a Cellette bench. This will also offer further legitimacy to the quality of this car's restoration once its completed.
        Click image for larger version  Name:	Cellette12.jpg Views:	0 Size:	169.7 KB ID:	113528
        As things sometimes workout, I was taking delivery of an old Cellette MUF7 several years ago. My buddy Ric had bought several benches as a package from GK restorations after Gary Kempton passed and this bench was amongst them. Ric was moving and cleaning out so this one was shipped to me. The day it arrived pictured above. Bare, save for two cross beams and in extremely weathered condition but hey, it was a real Cellette bench. A very long way from mounting a 356 chassis to it so I had to do some research and hunting for the additional hardware it lacked.
        Click image for larger version  Name:	IMG_9214.jpg Views:	0 Size:	616.8 KB ID:	113529 Fast forward several years later and I had located and purchased the three additional beams it lacked. (It needed a pair of outrigger beams for the front and one more basic cross beam.)
        Click image for larger version  Name:	IMG_9215.jpg Views:	0 Size:	670.3 KB ID:	113530 As well as a set of original Cellette footings and all the needed hardware to mount the beams to the bench and then the footings to beams.
        Click image for larger version  Name:	IMG_9218.jpg Views:	0 Size:	614.8 KB ID:	113531 Through the years the bench was a storage shelf but now with some components to move forward it was cleared off to begin figuring out where these crossbeams and footings needed to mount for a 356 application.
        Click image for larger version  Name:	IMG_9220.jpg Views:	0 Size:	640.4 KB ID:	113532 Based on a factory Cellette diagram and various photos found on the web I was able to dial in their position.
        Last edited by JTR70; 12-31-2022, 04:41 AM.
        Justin Rio

        Comment


        • Click image for larger version  Name:	IMG_9221.jpg Views:	0 Size:	628.8 KB ID:	113534 This bench sat out in the Florida elements for at least several seasons so the bolts holding the pair of beams on it when this bench arrived were completely rust frozen. I tried several rounds of penetrating oil and torch heat but the Allen heads stripped out on me before they gave up. I then had to drill the bolt heads out and hammer the beams upward and over the bolt shanks. A true PIA as they are a snug machine fit but I eventually got them both dismounted. Just getting ready to free this last rear beam so it could be cleaned and turned around for a 356 application. Click image for larger version  Name:	IMG_9225.jpg Views:	0 Size:	565.6 KB ID:	113535 Rear beam cleaned, flipped over and with rear trans hoop mount footings in position. BTW; all hardware was thoroughly greased as I never want to deal with frozen bolts on this rig again.
          Click image for larger version  Name:	IMG_9226.jpg Views:	0 Size:	636.8 KB ID:	113536 These beams are deceptively heavy and weigh every bit of 85+ lbs. each. Actually everything is very beefy as it should be for frame straightening but care really had to be taken while working with these planks alone.
          Click image for larger version  Name:	IMG_9228.jpg Views:	0 Size:	577.7 KB ID:	113537 3/4 of the way there...
          ​Bench now ready for the 356 specific fixtures. That next...

          Thanks for looking!

          Justin
          Last edited by JTR70; 12-31-2022, 04:21 AM.
          Justin Rio

          Comment


          • New 356 fixtures from RD
            Click image for larger version  Name:	IMG_9318.jpg Views:	0 Size:	628.2 KB ID:	113539 Stepped up and purchased a set of fixtures from RD. A very nice kit, big, heavy with clean machined parts. A lot of machine time invested for precision so I could further appreciate the rather large price tag for this set. Actually it was all very expensive, each additional plank I had to buy was just under a grand each and the footing set was 650.00 which was a very good deal. All totaled it was quickly approaching 10K to finish outfitting this bench for a 356. Glad this hunt was over!
            Click image for larger version  Name:	IMG_9628.jpg Views:	0 Size:	219.3 KB ID:	113540 Bench now moved into position under the body. I lucked out again as my rotisserie configuration allowed just enough room to maneuver it underneath.
            Click image for larger version  Name:	IMG_9632.jpg Views:	3 Size:	213.2 KB ID:	113541 Started at the back and lowered the body down onto the rear torsion housing mounts first. This would allow the front of the body to pivot from there as I lowered the front end down off of the rotisserie with my cherry picker. Lucked out again as all these contraptions had space to overlap and work keeping this a one-man operation. Hard to tell in this shot but the front torsion housing was going to over shoot the pins by well over an inch; not due to old accident damage BTW. This would be a discovery adjustment and part of the learning process as it went.
            Click image for larger version  Name:	IMG_9637.jpg Views:	0 Size:	222.7 KB ID:	113542 Lowered down fully and officially off of the rotisserie and onto the bench but the front just resting on a bottle jack at this point as again, the locating pins where well out of range. The body mounting continues...

            Thanks for looking!
            Justin
            Last edited by JTR70; 12-31-2022, 06:50 PM.
            Justin Rio

            Comment


            • Dialing in the footings:
              Click image for larger version  Name:	IMG_9222.jpg Views:	0 Size:	595.8 KB ID:	113544 As you can see the receptacles in the footings are not centered but indexed to one side and can potentially be mounted 4 different ways onto the planks. My initial setting for all four of these bases was as pictured with the receptacles oriented to the front. Being very green to the world of cellette bench set up this seemed like the best position as near as I could tell. Once the car was mounted at the rear torsion housing this position placed the body too far forward by about an inch and over shot the front jigs by about that distance. The forward trans mount fixtures (second plank here) would not reach the flanges on the housing by about the same distance further confirming this was not correct. Next stab at it was to rotate the rear torsion tube footings by 180 degrees placing the receptacles to the back. The body was now too far back by about an inch. The front beam was now behind the jig pins by well over an inch! This couldn't be right either. No way had that beam been shoved back a full inch. There is not enough deformation in the chassis to account for that much movement. When I tried installing the trans mount jigs they were completely crowded out no matter how the base was rotated so this orientation proved incorrect as well.
              Click image for larger version  Name:	IMG_9638.jpg Views:	0 Size:	250.2 KB ID:	113545 After the first two positions where gamed out I was onto a lateral orientation pictured above.
              Click image for larger version  Name:	IMG_9640.jpg Views:	0 Size:	243.1 KB ID:	113546 This orientation turned the trick almost immediately. The forward trans mounts locked into position with the mounting pins. Since the back of the car is damage free this is the baseline. All that mattered at the moment was that it all mounted and lined up back here first...and it was.
              Click image for larger version  Name:	IMG_9636.jpg Views:	0 Size:	189.4 KB ID:	113547 The front misalignment was now showing a more realistic and expected distance with the pins which reflected the deformation in the chassis. Not a full inch back as I was seeing on my second try.
              Click image for larger version  Name:	IMG_9635.jpg Views:	0 Size:	174.5 KB ID:	113548 Left side was just a few MM's back too. Again being new to all of this I was still a bit in doubt if I had the car on there correctly so that evening I went back on the web looking for more confirmation photos with a new base of experience from the days session.

              More to come...

              Thanks for looking!

              Justin
              Last edited by JTR70; 01-01-2023, 01:58 AM.
              Justin Rio

              Comment


              • Body finally jigged and set on the bench.
                Click image for larger version  Name:	IMG_9638.jpg Views:	0 Size:	250.2 KB ID:	113550 After an evening of photo research on the web I was able to confirm that yes, this lateral orientation of the rear torsion footing was correct.
                Click image for larger version  Name:	IMG_9639.jpg Views:	0 Size:	228.0 KB ID:	113551 Here was a new problem that cropped up. The locking pin hole that establishes the fixtures height and orientation into the footings receptacle was now 90 degrees out. Had I not found confirmation on the web that this configuration was correct I would have been thrown for a loop. Considering this is a reproduction fixture set this is just an oversight. This hole was just indexed wrong when the shank was weld on; an easy mistake to make as the rest of the fixtures shanks/locking pins are oriented this way. IE front to back.
                Click image for larger version  Name:	IMG_9646.jpg Views:	6 Size:	241.4 KB ID:	113552 The simple solution was to run this pair of fixtures up to my machinist to add an additional locking pin hole in the correct 90 degree offset. My first thought was to tap an intersecting hole but that I feared would weaken the shank too much. Fortunately the footings have a secondary hole so Bill calculated its distance to preserve the fixtures original height and orientation but now utilizing the lower pin hole in the base.
                Click image for larger version  Name:	IMG_9647.jpg Views:	6 Size:	243.2 KB ID:	113553 At last the car was finally mounted on the bench correctly. Back end is jigged and locked in so I can now work my way forward and accurately highlight and locate the front beam. I'll show that next.

                Thanks for looking!

                Justin
                Last edited by JTR70; 01-01-2023, 06:37 PM.
                Justin Rio

                Comment


                • Justin,

                  I have often wondered about how to set up the Cellette. Your photos are so good, its no easy task unless as you have managed to obtain all the parts! You have done so well there and you can now be certain on seeing errors!! Really impossible to be sure without that fixture . In fact so hard to know what you buying with a 356 unless you have all that gear. I think it really was money well spent Justin expensive for sure but you can check anything with no guessing!! Also I guess its always a very saleable item in the future and would suit those involved with 356 repair work like you always are attempting.

                  Such an interesting thread this one, just like all your others. Hope others can see this sort of info is so important to 356 restoration its very rare to see it so closely detailed !
                  Well done and thanks!

                  Roy

                  Comment


                  • JTR70
                    JTR70 commented
                    Editing a comment
                    Thank you Roy and again always great to know that these posts are of some use and interest. I did want to share and dispel any voodoo or black magic that seems to surround this system at times. Its just a frame dozer at the end of it all but as you stated the dedicated jigs do and will highlight any slight misalignment that could go undetected otherwise (which I'll show next). Yes, a big investment but as you stated, very saleable down the road but in the meantime it gives me the capability to rebuild a future chassis that's severally bent, in two pieces or entirely from scratch...and not just an old 356 BTW. I've always been interested in building off-road tube chassis like my buddy Warren and this bench gives me a solid foundation to pursue that...
                    Thanks again Roy and Happy New year to you! Justin
                    Last edited by JTR70; 01-02-2023, 05:53 PM.

                • How much was the front beam of this car shifted?
                  Click image for larger version  Name:	IMG_9645.jpg Views:	0 Size:	220.0 KB ID:	113557 Now that I had the back end of this car set in the jigs I was very curious to know just how far out the front beam of this car actually was from factory specifications. To get an idea I ran masking tape around the perimeter of the front fixture bases to mark their footprint while bolted down in their set location on the beams. The fixtures where then unbolted from the beams so I could install the pins into the torsion housing to see how far off the bases where in relation to the masking tape.
                  Click image for larger version  Name:	IMG_9644.jpg Views:	0 Size:	186.8 KB ID:	113558 Not nearly as bad as it seems. Maybe 5MM worth of difference.
                  Click image for larger version  Name:	IMG_9643.jpg Views:	0 Size:	201.7 KB ID:	113559 As well as being back the beam is also slightly cocked upward on this side. This is one of those detials that could go unoticed without these jigs Roy.
                  Click image for larger version  Name:	IMG_9641.jpg Views:	0 Size:	187.1 KB ID:	113560 The left side is also back but not as far. It angles slightly to the right as would be expect with the right side pushed back. Technically this is nothing and could all be compensated for in the final wheel alignment. This car would track straight down the road just fine if left alone but since we're here and have the tools will pull it out back into factory specs.
                  Click image for larger version  Name:	IMG_9651.jpg Views:	0 Size:	196.9 KB ID:	113561 In preparation to pull the beam out I'm going to begin removing a bit more "connective tissue" in and around it to make the eventual pull correction a little easier on everyone. Besides this outer layer of steel running around the tubes needs to be peeled back anyway to get at the last remnants of the battery box side wall underneath it. This coming up next.

                  Thaks for looking!

                  Justin
                  Last edited by JTR70; 01-03-2023, 12:23 AM.
                  Justin Rio

                  Comment


                  • Justin , I now know more about a Cellette mounting table than I ever knew. If I were a little closer I would pop over to see this for myself. Well done on explaining it is not easy at all. Now I need to see how you are going to pull it out !! Where to place equipment to do that? Its been an eye opener to see this work in operation.

                    Super Justin !
                    Roy

                    Comment


                    • JTR70
                      JTR70 commented
                      Editing a comment
                      I wish you were closer too Roy, you'd always have an open initiation to stop by old friend. I don't have the fancy cellete pulling arm unit but I'll come up with a anchor/come along contraption to pull it out. as you can it doesn't have to go very far.

                  • Justin

                    Do you have the VW 256 to check the alignment of the tubes? If not I have one I can send down to you. Tom Perazzo use it to check his 356, and posted a video on using it.
                    Pushed around since 1966.

                    Comment


                    • JTR70
                      JTR70 commented
                      Editing a comment
                      PM sent John. Thanks again! Justin
                      Last edited by JTR70; 01-10-2023, 09:25 PM.

                  • Front tube area prep:
                    Click image for larger version  Name:	IMG_9661.jpg Views:	0 Size:	1.61 MB ID:	113568 Going after this last remnant of OG battery box side wall.
                    Click image for larger version  Name:	IMG_9657.jpg Views:	0 Size:	211.2 KB ID:	113569 Last portion of the actual frame "wall" overlaps it and terminates here. In process of drilling out the last remaining spot welds. There where of course a few.
                    Click image for larger version  Name:	IMG_9658.jpg Views:	3 Size:	205.8 KB ID:	113570 Lower portion of the frame "wall" drilled free and peeled back behind the tubes and out of the way revealing the rest of that old wall. Heading upward to free the rest of it.
                    Click image for larger version  Name:	IMG_9666.jpg Views:	3 Size:	213.0 KB ID:	113571 My intention was to save a straighten this side of the battery box wall out and I'd still like to do that but we'll have to see as this repair and pull progresses.
                    Last edited by JTR70; 01-10-2023, 09:40 PM.
                    Justin Rio

                    Comment


                    • Click image for larger version  Name:	IMG_9665.jpg Views:	0 Size:	222.2 KB ID:	113573 New battery box is here and as you can see it came preassembled. However, the way the side walls are lapped over it would be far easier and cleaner if this rear bulkhead wall was out of my way.
                      Click image for larger version  Name:	IMG_9667.jpg Views:	0 Size:	200.0 KB ID:	113574This standard offering is incorrect for a T2 BTW. The battery recess in the wall is the narrower T1 version. Original T2 version laying on the floor above. This detail was discussed here: Evolution of the 356A T1 & T2 How they differ - ABCGT Forum
                      Click image for larger version  Name:	IMG_9668.jpg Views:	0 Size:	175.8 KB ID:	113575This T2 wall's recess is about an inch wider and slightly asymmetrical to compensate for the additional width allowing it to mount in between the standard and unchanged front beam flanges. I'll be repairing donating this wall for the project so naturally this new battery box unit will be coming apart for both correction and installation.
                      Click image for larger version  Name:	IMG_9653.jpg Views:	0 Size:	195.1 KB ID:	113576 Front lower gusset removal: My initial plan was to repair the bottom of this gusset and leave the remains alone but I want this beam as unsecured as possible in preparation for an easy correction pull.
                      Click image for larger version  Name:	IMG_9654.jpg Views:	0 Size:	214.8 KB ID:	113577 Gusset remains easily removed as the middle portion of the spots had given up which is rare. As you can see I stopped welding the new flange at the front bulkhead in preparation for the eventual beam pull. Only this single unflanged portion of this old wall is now maintaining this beams position. This is now going to be a very easy pull back out into factory specs. Once its there all the strength and integrity will be added back in.

                      Thanks for looking!
                      Justin
                      Last edited by JTR70; 01-10-2023, 10:19 PM.
                      Justin Rio

                      Comment


                      • I remember Justin reading that thread about the difference in Battery width location beween T1 and T2. Lets hope it it all pulls out okay and the modification to the battery box goes okay too.

                        Roy

                        Comment


                        • JTR70
                          JTR70 commented
                          Editing a comment
                          It should Roy, just another little detour along the way of getting the build details correct.

                      • Checking the front beam assembly for parallel.

                        We know the front beam has been shifted a touch in the chassis but the next step was to make sure the twin beam assembly itself was still running square. John Brooks was generous enough to loan us his Factory VW-256 tube gauge.
                        Click image for larger version  Name:	IMG_9674.jpg Views:	3 Size:	207.6 KB ID:	113615 The tool arrived nicely packaged in its old original wooden box. My machinist has purchased many German cutting heads and specialized tooling throughout his career and aside from the quality what stood out to him was the beautifully crafted wooden box they would all come in. Same thing rings true here. Note the twin collars on the lid for a 356 application.
                        Click image for larger version  Name:	IMG_9675.jpg Views:	0 Size:	211.1 KB ID:	113616 Initial mock up with the checking plate resting on the plank here. Realized that inner bushing had been removed so no way of getting an accurate reading this time around. Click image for larger version  Name:	IMG_9709.jpg Views:	0 Size:	173.9 KB ID:	113617 New bushing set arrived a few days later. These new urethane versions should hold up a lot better than the old bakelite units.
                        Click image for larger version  Name:	IMG_9715.jpg Views:	0 Size:	478.0 KB ID:	113618 New bushings installed with a venier of lithium grease on the contact surfaces for ease of installation. Checking plate resting on the reference surfaces.
                        Click image for larger version  Name:	IMG_9714.jpg Views:	0 Size:	457.7 KB ID:	113619Much to my surprise I could generate no detectable rocking motion in this plate; I was expecting at least a little movement.
                        Last edited by JTR70; 01-24-2023, 11:13 PM.
                        Justin Rio

                        Comment

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